全球及地区市场新闻海上前沿

Trillion Energy 提供 SASB 速度管柱安装更新

Trillion Energy 提供了西南黑海 SASB 气田速度管柱安装程序的最新进展。目前,2-3/8 英寸生产油管(速度管柱或 VS)正在下入 Guluc-2 井。安装 VS 的目的是减少 SASB 气井的水负​​荷问题。

10 月 27 日,压井装置被安置在 Akcakoca-3 井上方,2-3/8 英寸 VS 通过现有的 4-1/2 英寸油管被送入井中。该作业于 10 月 29 日完成。作业期间,井内持续流动。

安装 VS 后,Akcakoca-3 的产量从大约 200 万立方英尺/天(安装前 27 天的平均产量)增加到 260 万立方英尺/天(安装后前 4 天的平均产量)。我们目前仍在监测油井的产量。

10 月 30 日,使用压井装置将 2-3/8 英寸速度管柱下入西阿克恰科卡 1 号井。该作业于 11 月 1 日完成,速度管柱的总测量深度达到 3,496 米。西阿克恰科卡 1 号井在作业前没有产气,预计在应用氮气刺激后将恢复天然气生产。

原文链接/DrillingContractor
Global and Regional MarketsNewsThe Offshore Frontier

Trillion Energy provides update on SASB velocity string installation

Trillion Energy provided an update on the velocity string installation program at the SASB gas field in the Southwestern Black Sea. Currently, 2-3/8” production tubing (velocity string or VS) is being run into the Guluc-2 well. The VS are being installed with the objective of reducing water loading issues in the SASB gas wells.

On 27 October the snubbing unit was positioned over the Akcakoca-3 well where 2-3/8” VS was run into the well through the existing 4-1/2” tubing. The operation was completed on 29 October. The well continued to flow throughout the operation.

Following the VS installation, Akcakoca-3 production increased from approximately 2 million cu ft/day (average production for the 27 days prior to installation) to 2.6 MMcf/d (average production first 4 days post VS). We continue to monitor production from the well at this time.

On 30 October, a 2-3/8” velocity string was run into the West Akcakoca-1 well using the snubbing unit. The operation was completed by 1 November, where the velocity string reached a total measured depth of 3,496 m. The West Akcakoca-1 well was not producing prior to the operation and gas production is expected to resume following nitrogen stimulation being applied.