88 Energy Limited 公布有关 Hickory-1 流量测试结果的更多信息

来源:www.gulfoilandgas.com 2024 年 4 月 19 日,地点:北美

重点介绍
“Hickory-1 的双重成功,轻油从 USFS 和 SMD 油藏流出。
”流动后测试研究即将开始,包括确保额外的潜在资源估算。
“同时考虑的商业化选项,包括外包给战略开发合作伙伴和/或早期的轻资本开发。

88 Energy Limited(88 Energy 或公司)很高兴提供有关 2024 年 4 月 2 日至 4 月 15 日宣布的、来自该公司位于项目的 Hickory-1 发现井的成功流量测试结果的进一步更新和信息位于阿拉斯加北坡的凤凰城(88 Energy ~75% WI 所有者)。

正如所宣布的,从 USFS 和 SMD-B 油藏中回收了轻质油,每项测试的关键细节总结如下,并对报告的结果进行了补充说明。

上部 SFS (USFS) 流动测试结果
——通过单次裂缝阶段 241,611 磅支撑剂体积对上部 SFS 储层中 20 英尺的射孔层段进行增产。
该井进行了清理并总共流动了 111 小时,其中自然回流 88 小时,氮气提升 23.5 小时。在 88 小时的自然回流期中,包括约 78 小时的清理工作以及在此期间回收的微量油,以及约 10.5 小时的既定生产期。

在既定的 10.5 小时生产期内,该井在自然回流期间平均石油流量约为 42 桶/天,总共生产了约 19 桶石油。在清理/非建立生产期间还回收了大约 6 桶石油。
”USFS 测试以超过约 70 bopd 的峰值流量进行生产,这是通过油罐容积在回流期间计​​算的瞬时流量在 30 分钟内测量了 1.55 桶。
”回收了多个油样,测得的油比重在 39.9 至 41.4 API 之间(代表轻质原油)。
SMD-B 流动测试结果
——SMD-B 储层中 20 英尺的射孔层段通过单次裂缝阶段 226,967 磅支撑剂体积进行增产。
该井经过清理并在氮气举升下总共流动了 84 小时,在油流到地面之前需要约 68 小时的清理时间,油流良好的时间需要约 16 小时。

最初石油到达地面后,该井的平均产油量为 4%,随着该井继续以约 170 桶/天的受控流体流量进行清理,在 16 小时内观察到的瞬时产量发生变化。计算出约 4 桶石油减产后回流期间的总体积。SMD
-B 测试以约 50 bopd 的计算峰值流量进行生产,这是回流期间计​​算的瞬时流量通过测量观察到的油含量和流体流速。
回收了多个油样,测得的油比重在 38.5 至 39.5 API 之间(代表轻质原油)。

远期计划
在 Hickory-1 发现井成功进行流量测试后,88 Energy 将重点关注:“完成 Hickory-1 井后测试和分析;
”确保 SFS 和 SMD 油藏的应急资源;
“ � 启动正式的外包流程,吸引高质量的新合作伙伴,为下一阶段的评估和开发提供资金;
早期生产系统的提前规划和设计
公司期待向股东通报测试后分析的最新情况。本公告已经董事会授权。

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原文链接/gulfoilandgas

88 Energy Limited Announces Further Information on Hickory-1 Flow Test Results

Source: www.gulfoilandgas.com 4/19/2024, Location: North America

Highlights
• Dual success at Hickory-1 with the flowing of light oil from the USFS and SMD reservoirs.
• Post flow test studies to commence including the securing of additional Contingent Resource estimates.
• Commercialisation options to be considered in parallel, including farm-out to a strategic development partner and/or early and a capital-lite development.

88 Energy Limited (88 Energy or the Company) is pleased to provide a further update and information in relation to the successful flow test results announced on 2 April and 15 April 2024, from the Company’s Hickory-1 discovery well, located in Project Phoenix on the North Slope of Alaska (88 Energy ~75% WI owner).

As announced, light oil was recovered from both the USFS and SMD-B reservoirs, with key details from each test summarised below, and to provide additional clarification on the reported results.

Upper SFS (USFS) Flow Test Results
• A 20ft perforated interval in the Upper SFS reservoir was stimulated via a single fracture stage of 241,611 lbs proppant volume.
• The well was cleaned-up and flowed for 111 hours in total, of which 88 hours was under natural flow back and 23.5 hours utilising nitrogen lift. Of the 88 hours of natural flow back period included ~78 hours of clean up with trace oil recovered during this time, and a period of ~ 10.5 hours of established production.

• During the established production period of 10.5 hours the well produced at an average oil flow rate of ~ 42 bopd during the natural flow back period, producing a total of ~ 19bbls of oil. Approximately 6bbls of oil was also recovered during the clean up / non-established production period.
• The USFS test produced at a peak flow rate of over ~70 bopd, which was an instantaneous rate calculated during flow back period via an oil tank volume measurement of 1.55 bbls over a 30 minute period.
• Multiple oil samples were recovered with measured oil gravities of between 39.9 to 41.4 API (representing a light crude oil).
SMD-B Flow Test Results
• A 20ft perforated interval in the SMD-B reservoir was stimulated via a single fracture stage of 226,967 lbs proppant volume.
• The well was cleaned-up and flowed for 84 hours in total under nitrogen lift, with ~68 hours of clean up prior to the flowing of oil to surface, with the well flowing oil over ~16-hour period.

• The well produced at an average oil cut of 4% following initial oil to surface, with instantaneous rates observed during the 16-hour period varying as the well continued to clean up at managed fluid flow rate of ~170 bbls/d with a calculated total volume during the flow back period following establishment of oil cut of ~4 bbls of oil.
• The SMD-B test produced at a calculated peak flow rate of ~50 bopd, which was an instantaneous rate calculated during the flow back period via a measurement of observed oil cut and fluid flow rates.
• Multiple oil samples were recovered with measured oil gravities of between 38.5 to 39.5 API (representing a light crude oil).

Forward Plan
Following the successful flow testing at the Hickory-1 discovery well, 88 Energy will be focused on: • Completing post-well testing and analysis at Hickory-1;
• Securing a contingent resource for the SFS and SMD reservoirs;
• Commencing a formal farm-out process to attract a high-quality new partner to fund the next stage of appraisal and development; and
• Advance planning and design of an early stage production system.
The Company looks forward to updating shareholders on the post test analysis. This announcement has been authorised by the Board.

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