下一口井的动员工作已经开始。

来源:www.gulfoilandgas.com,2025年11月17日,地点:南美洲

Melbana Energy Limited(简称“Melbana”或“公司”)就其作为作业者并持有30%权益的古巴陆上9号区块生产分成合同(PSC)项目发布以下运营更新。

要点
:- Amistad-11井的动员工作已启动。-
钻井工作将于本月底前开始,并在年底前完成,但需获得必要的许可证和批准。-
Amistad-11井将与Alameda-21井形成姊妹井,采用上倾钻井方式,并运用基于以往经验开发的最新井设计和地层管理技术。Melbana

Energy执行主席Andrew Purcell评论道:“全面分析Amistad-2井的钻探结果需要一些时间,因此我们正在调动钻机,以便在获得最终批准的同时,做好钻探Alameda-2生产井姊妹井的准备。” Alameda-2井最初日产量超过1200桶原油,但由于我们在钻探Alameda-3井时破坏了地层,导致该井停产,而我们尝试的修井作业也仅取得部分成功。在已知高产油井的上倾位置新建一口井,并结合我们以往在管理此类地层和完井方面积累的所有经验,我们非常有信心在年底前以更高的产量投产。临时转向新井需要巧妙的配合,在此我衷心感谢我们经验丰富的运营和许可团队以及所有积极响应这一计划的合作伙伴。Melbana及其合作伙伴已批准将钻井平台迁移至9号区块,以便钻探下一口生产井,该井将被命名为Amistad

-
11。

Amistad-11 将在 1 号井场钻探(见第 2 页图 1),紧邻自 2025 年 4 月以来一直在生产的 Alameda-2 井。大约一周前,Amistad-2 相关活动结束后,钻机一直停留在附近的 4 号井场,周末期间已下达了调动钻机的指令。


根据最终许可和批准的到位时间,预计Amistad-11井将于2025年11月底前开钻,随后需数周时间钻至总深度。完井和测试作业将在之后进行,之后该井将投入生产。

此前计划的下一口井是Amistad-3,位于9号井场附近。现在决定先钻一口高置信度井,以便研究Amistad-2井的钻探结果,并根据由此获得的经验教训检验Amistad-3井的钻探计划。Amistad

-11井的目标
:Amistad-11井计划与Alameda-2井并列钻探——Alameda-2井是该公司迄今为止在9号区块最成功的生产井。Alameda

-2井钻遇了一个已知的储层段(Amistad上部1B单元),并产出比古巴通常开采的原油更轻(19° API)、更低粘度(30 cP2)的原油。该井的峰值产量为1903桶/日³(稳定平均产量为1235桶/日)⁴。根据这些结果,公司独立资源认证机构对1B单元或有石油储量的最佳估算(P50)为3.31亿桶石油,或有(可采)资源量为4600万桶石油⁵,⁶。

在成功评估该发现后,Alameda-2井被关闭,以便在同一井场附近钻探Alameda-3井。2023年底重新开启Alameda-2井时,发现其产量已降至300桶/日以下⁷。对测井、岩心和其他数据的分析表明,用于关闭该井的流体可能对井筒附近的岩层造成了损害。为修复此次损害,我们借鉴了古巴国家石油公司处理类似问题的经验,并参考了对不同类型和成分的流体与1B单元地层样品相互作用的研究结果,制定了一项修井方案。该修井方案成功地将日产量提高到488桶,但由于盐水和酸液渗漏到地层中,计划的全部内容未能执行<sup>8</sup>。自修井完成以来,Alameda-2井一直保持生产,截至2025年9月30日,已生产超过36,000桶原油<sup>9</sup>。

我们曾考虑对Alameda-2井进行另一次修井,或者重新进入井筒钻一侧钻井,但考虑到这些方案的价值和风险,以及结合公司已开发并应用于当前作业实践的所有流体管理和井筒设计经验新建一口井,我们认为新建一口井更有可能实现预期目标。Amistad

-11井设计
Amistad-11井的钻井计划是在Alameda-2井的上倾方向钻一口双井,该井从较浅的深度开始钻进,以在最佳储层深度实现所需的层间分离,然后继续钻至1B单元下部1000米(MD)的总深度(见图2)。该井计划采用裸眼完井,但如有需要,也可下入开槽式生产衬管。

鉴于Amistad-2井良好的钻速和高产能完井效果,Melbana公司根据其此前在该地层管理经验开发的储层钻井液将再次用于Amistad-11井。考虑到迄今为止的产量相对于根据先前测试估计的可能总可采储量而言较小,以及该井位于Alameda-2井连通区域之外,预计所选井位和井眼轨迹造成的排水干扰也将降至最低。

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原文链接/GulfOilandGas

Mobilisation commenced for next well

Source: www.gulfoilandgas.com 11/17/2025, Location: South America

Melbana Energy Limited (Melbana or Company) provides this operational update regarding Block 9 PSC onshore Cuba, for which it is operator and holds a 30% interest.

Highlights
- Mobilisation commenced for Amistad-11.
- Drilling to begin before the end of the month and complete before year end, subject to formal completion of necessary permits and approvals.
- Amistad-11 to twin Alameda-21, up-dip and using latest well design and formation management techniques developed using previous learnings.

Melbana Energy’s Executive Chairman, Andrew Purcell, commented: “It will take some time to fully analyse the results of Amistad-2, so we’re moving the rig to be ready to drill a twin of the Alameda-2 production well whilst we secure final approvals. Alameda-2 originally produced at more than 1200 barrels of oil per day, but we damaged the formation shutting it in to drill Alameda-3 and the workover we tried was only partially successful. A new well updip of a known successful producer, incorporating everything we’ve learned about how to manage these formations and complete our wells, gives us high confidence that this can be brought online at an improved rate before the end of the year. The last-minute pivot to a new well has taken some deft footwork, so my sincere thanks to our experienced operations and permitting teams as well as our partners, all of whom have responded proactively to this initiative.”

Amistad-11 Production Well
Melbana and its partners have approved the relocation of the rig to allow the drilling of the next production well in Block 9, to be designated Amistad-11.

Amistad-11 is to be drilled off Pad 1 (see Figure 1 on page 2), immediately adjacent to the Alameda-2 well that has been on production since April 2025. Instructions to mobilise the rig, which has remained nearby on Pad 4 following the completion of Amistad-2 related activities about a week ago, were given over the weekend.


Subject to the timing of receipt of final permits and approvals, it is expected that Amistad-11 should spud before the end of November 2025 and then take a few weeks to drill to total depth. Completion and testing operations would follow before leaving the well on production.

It was previously planned for the next well to be Amistad-3, drilled off Pad 9. It has now been decided to next drill a high confidence well to allow for the results of Amistad-2 to be studied to allow the plans for that well to be tested against any of the resultant learnings.

Amistad-11 Objectives
Amistad-11 is planned to twin Alameda-2 - the Company’s most successful production well to date in Block 9.

Alameda-2 intercepted a known reservoir section (Unit 1B in the upper Amistad sheet) and flowed a significantly lighter (19° API), lower viscosity (30 cP2) oil to surface than is typically recovered in Cuba. The well flowed at a peak rate of 1903 BOPD3 (stabilised average flow rate of 1235 BOPD)4. Given these results, the Company’s independent resource certifier’s gross best estimates (P50) for contingent oil in place in Unit 1B volume is 331 million barrels of oil with a contingent (recoverable) resource of 46 million barrels of oil5,6.

Following the successful appraisal of this discovery, Alameda-2 was shut in to allow the drilling of Alameda-3 nearby off the same pad. Upon reopening Alameda-2 in late 2023 it was discovered that its production rate had dropped to less than 300 BOPD7. Analysis of logs, cores and other data concluded that the fluids used to shut in the well may have damaged the formation near the well bore. A workover program to try and repair this damage was designed using the experience of the Cuban national oil company with similar issues as well as using the results from studies examining the interaction of various fluid types and compositions with formation samples taken from Unit 1B. The workover program successfully increased the production rate to 488 BOPD, but the entire scope of the planned program was unable to be executed due to brine and acid losses to the formation8 . Alameda-2 has remained on production since completion of the workover and had produced more than 36,000 barrels of oil as of 30 September 20259.

Consideration was given to conducting another workover of Alameda-2, or re-entering it and drilling a sidetrack, but when the value risked outcomes of these alternatives were considered alongside a new well incorporating all the fluid management and well design learnings the Company has developed and incorporated into its current operational practices, it is believed a new well provides the highest probability of achieving the desired outcomes.

Amistad-11 Well Design
The plan for Amistad-11 is to drill an up-dip twin of Alameda-2 that kicks off at a shallower depth to achieve the desired separation at optimum reservoir depth then to drill on to a total depth of 1000 m.MD in the lower section of Unit 1B (see Figure 2). The well is planned to have an open hole completion, but with the capability of running a slotted production liner, if required.

The reservoir drilling fluid Melbana has developed in response to its experience managing this formation previously will once again be used, given the good drilling rate of penetration and high productivity completion observed at Amistad-2. Drainage interference from the selected well position and trajectory is also estimated to be minimal, given the small volume produced to date relative to likely total recoverable volume estimated from prior testing and location outside the communication area of Alameda-2.

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