人工举升

案例研究:DJ盆地运营商使用原型井下工具提高产量,减少成熟油井中的天然气干扰

现场结果表明,重新思考油管锚捕集器设计可以减少气体干扰并支持后期生产。

一种新型的纤薄型管锚固定器。来源:TechTAC。
一种新型的纤细型管锚固定器。
来源:TechTAC。

一家在丹佛-朱尔斯堡(DJ)盆地运营的私营勘探和生产(E&P)公司,由于该盆地的气油比(GOR)呈上升趋势,因此在提高其成熟油井的产量方面面临困难。

这家勘探开发公司面临的挑战之一在于如何最大限度地提高成熟油井人工举升的效率,而这本身就存在经济效益问题。一旦油井产量急剧下降,投资昂贵的增产技术或设备往往就缺乏经济意义。如果油井像该地区许多油井一样,在泵上方使用标准的油管锚捕集器(TAC),那么即使是安装简单的气体分离器等较为适度的投资也可能收效甚微。

十多年来,人们已经认识到,传统的B2型TAC(环形锚杆)会在井内形成阻塞点,因为锚杆外径(OD)与套管内径(ID)之间的环形空间非常小(URTeC 1918491)。在许多情况下,阻塞点会导致井壁堵塞、地层气体滞留,并在井内造成显著的压力下降,从而加速结垢

可能的解决方案,特殊情况

虽然细长型TAC已被证明能有效允许地层气体绕过锚杆并沿井环空向上流动而不影响生产,但有时内径较小的TAC可能与公司首选的井筒设计不兼容。例如,过量的砂层或区域性偏好等因素会影响油管锚杆在井下的具体位置。

对于这些外径为 5.5 英寸的成熟井,作业者选择使用 2 英寸油管来配合大型泵,并要求将 TAC 安装在泵座接头上方,泵通过该 TAC 运行。使用 2 英寸内径的油管时,5.5 英寸的“极限”TAC 可以安装在泵的上方或下方,但当使用 2 英寸油管时,只能安装在泵的下方。

这意味着该运营商必须在其油井中使用标准的B2型TAC,这反过来又导致了气体干扰和堵塞的问题。这家油气勘探开发公司希望找到一种既能满足油井设计要求,又能促进更好的流体通过,从而最大限度降低气锁风险的解决方案。

纤细的锚,带全通径内径

生产公司与技术开发商合作,选择测试一种新型TAC系统。该锚杆采用了一种新颖的设计,使其周围拥有更大的流通面积,同时内径仍足够大,可供设计用于2½英寸油管的杆式泵通过。如果测试成功,新型TAC将有助于减少气体干扰,提高三口成熟油井的产量,同时满足安装在井口接头上方的要求。

2024年9月,三个原型锚被制造出来,并通过油田设备供应商运送给生产公司。到11月中旬,所有三个TAC(终端锚固装置)均已下井并投入生产。每个锚都安装在泵座接头上方,泵通过该接头运行。

早期结果:部署后 0 至 30 天

据勘探开发公司称,钻井平台作业人员在使用原型TAC时未遇到任何问题。其中一个锚杆在下水后不久确实需要拆除,但这并非TAC本身存在缺陷,而是因为油管出现了破损。

然而,这次意外拆卸却让钻井队有机会测试重新安装并释放TAC装置,整个过程顺利完成。勘探开发公司报告称,TAC装置的安装和释放都很简单,安装和拆卸过程中均未遇到任何问题。

勘探与生产部门还注意到,井口天然气排放量显著增加,这表明锚杆的纤细设计在解决5.5英寸套管井的天然气干扰问题方面效果显著。具体而言,每口井的地面天然气排放量均增加了25%至30%。

此外,根据测力计数据,各井的泵送填充率均有所提高。勘探开发部门的生产人员报告称,改造为原型TAC装置的油井的泵送填充率有所提高,增幅通常在15%至25%之间。

长期影响:部署后 1 至 6 个月

在接下来的 5 个月里,这三口成熟油井继续生产,无需任何修井或干预。

TAC持续保持生产管柱的张力,从而实现高效作业并避免不必要的磨损。尽管DJ盆地该区域的天然气含量较高(East Daley Analytics,2025),但井口产气量持续增加,降低了气锁风险。

然而,最显著的益处体现在产量的提高上。除了使用新的原型锚固装置外,这三口井的生产管柱没有做任何显著改动,每口井的日产量就从大约 40 桶增加到近 80 桶,增幅接近 100%。

对比研究

三口试验井产量的提高主要归功于纤细型锚杆提供的更大流通面积。近期一项独立的计算流体动力学 (CFD)研究对比了 5.5 英寸标准 B2 型锚杆和同尺寸的新型纤细型 TAC 原型锚杆。

该研究采用计算流体动力学(CFD)方法,比较了两种不同类型的5.5英寸油管锚捕集器周围环形空间内的气体流动情况。主要研究结果表明,标准型B2 TAC的动能湍流和涡量显著高于纤细型TAC。这种湍流会捕获地层气体,并导致水垢、石蜡和硫化铁沉积,其主要原因是标准型B2 TAC的流通面积小于纤细型TAC。

根据报告,图 1说明了“标准 TAC 中压力场的突变以及流场障碍物的潜在存在,预计会比[纤细型] TAC 在 TAC 沿线的流场中产生更大的湍流。”

图 1——传统系统与新型原型系统之间的湍流场行为。来源:TechTAC。
图 1——传统系统与新原型之间的湍流场行为。
来源:TechTAC。

报告还指出,“与[纤细型TAC]情况相比,标准TAC流场中的涡量强度预计会显著增强”,如图2所示,图中显示了强度在0.0001到0.005之间的涡量场。

图 2——计算机示意图,显示了工具之间的涡流场行为。来源:TechTAC。
图 2——计算机示意图,显示工具之间的涡流场行为。
来源:TechTAC。

结论

对于那些持续存在气锁或结垢问题,需要将TAC(气固连接件)置于井口接头上方的油井,一种新型的全通径细长TAC原型为传统的锚固方案提供了一种替代方案。在丹佛-朱尔斯堡盆地,一家油气勘探开发运营商采用了这种细长型TAC,即使在气油比高且持续上升的情况下,也实现了老井更高的产量。

延伸阅读

DJ Basin 转向天然气开采,East Daley Analytics。(2025 年)

URTeC 1918491 管锚可降低生产率和泵填充率, 作者:JN McCoy、OL Rowlan、CA Taylor 和 AL Podio。

布拉德·克里斯特是TechTAC的总裁兼所有者,该公司是一家油管锚固解决方案供应商,业务遍及美国多个主要盆地。克里斯特于2023年收购了该公司,此前他在关键材料管理公司Savage Companies工作了20多年,担任过多个领导职务。他最近担任该公司基础设施部门总裁,负责管理遍布美国、加拿大、墨西哥和沙特阿拉伯的约140个分支机构和2500名员工。他的从业经历包括管理炼油厂、石化厂和转运设施的运营。克里斯特拥有宾夕法尼亚大学沃顿商学院的工商管理硕士学位和杨百翰大学的经济学学士学位。

原文链接/JPT
Artificial lift

Case Study: DJ Basin Operator Uses Prototype Downhole Tool to Increase Production, Mitigate Gas Interference in Mature Wells

Field results highlight how rethinking tubing-anchor-catcher design can reduce gas interference and support late-life production.

A new slim-style tubing-anchor catcher. Source: TechTAC.
A new slim-style tubing-anchor catcher.
Source: TechTAC.

A privately held exploration and production (E&P) company operating in the Denver-Julesburg (DJ) Basin was facing difficulties boosting production from its mature wells as the basin’s gas‑to-oil ratio (GOR) trended higher.

Part of the E&P company’s challenge was inherent in the economics of maximizing the efficiency of mature wells on artificial lift. Once a well reaches a stage of steep production declines, investing in expensive stimulation techniques or equipment rarely makes financial sense. More modest investments, such as installing a simple gas separator, can also be largely futile if the well also uses a standard tubing anchor catcher (TAC) above the pump, as many of the region’s wells do.

For more than a decade, it has been recognized that traditional B2-style TACs can create a chokepoint within the well because the annular space between the anchor’s outside diameter (OD) and the internal diameter (ID) of the casing is so small (URTeC 1918491). In many cases, the chokepoint invites plugging, traps formation gas, and creates a significant pressure drop within the well, accelerating the formation of scale.

Possible Solutions, Unique Circumstances

While slim-style TACs have proven very effective at allowing formation gas to flow around the anchor and up the annulus of a well without disrupting production, situations may arise where a TAC with a reduced ID is not compatible with a company’s preferred well design. For example, factors such as excess sand or regional preferences can influence the specific downhole placement of a tubing anchor.

In the case of these mature wells with 5.5‑in. OD, the operator chose 2⅞-in. tubing to accommodate a large pump and required that the TAC be placed above the seat nipple with the pump running through it. With a 2-in. ID, a 5.5-in. “slim” TAC can be set above or below the pump with 2⅜‑in. tubing, but only below the pump when 2⅞‑in. tubing is used.

That meant this operator had to use a standard B2-style TAC in its wells, which in turn led to struggles with gas interference and plugging. The E&P company wanted to find a solution that could meet the design requirements of its wells while also promoting better flow-by to minimize the risk of gas locking.

A Slim Anchor With a Fullbore ID

Working with the technology developer, the production company chose to test a new TAC system. The anchor leverages a novel design that allows it to provide significantly more flow-by area around the anchor while still maintaining an ID large enough to allow rod pumps designed for 2⅞-in. tubing to pass through it. If successful, the new TAC would help to mitigate gas interference and increase production across three mature wells while meeting the requirement to be placed above the seat nipple.

Three prototype anchors were manufactured and shipped to the production company via an oilfield equipment supplier in September 2024. By mid-November, all three TACs were downhole and in production. Each was set above the seat nipple with the pump running through it.

Early Results: 0 to 30 Days After Deployment

According to the E&P company, the rig crew encountered no issues running in the prototype TACs. One of the anchors did have to be removed shortly after running in, but not because of a deficiency with the TAC. Rather, the tubing had a hole in it.

However, the unexpected removal did give the rig crew a chance to test releasing and then rerunning the TAC after it was redressed, which proceeded without incident. The E&P reported that the TAC was simple to set and release and that no issues were encountered during installation or removal.

The E&P also noted a significant increase in the volume of gas coming out of the wells, suggesting the anchor’s slim design was working well for gas-interference issues in wells with 5.5-in. casing. Specifically, the wells each saw a 25 to 30% increase in the volume of gas being discharged on the surface.

Additionally, pump-fillage rates improved in each of the wells, according to dynamometer card data. Production staff within the E&P reported increased pump fillage on wells that were converted to the prototype TAC, with increases typically ranging between 15 to 25%.

Longer-Term Impact: 1 to 6 Months After Deployment

Over the next 5 months, all three mature wells continued producing without any need for workovers or interventions.

The TACs continued to hold tension in the production string, enabling efficient operations and avoiding unnecessary wear and tear. The increased volume of gas coming off the wells remained consistent, mitigating the risk of gas locking, despite the gassier composition of this area of the DJ Basin (East Daley Analytics, 2025).

The most significant benefit, however, came in the form of increased production. Without making any notable changes to the production strings of these three wells other than using the new prototype anchor, each went from producing roughly 40 B/D to almost 80 B/D, marking a nearly 100% increase.

Comparison Study

The increased production experienced in the three test wells is largely tied to the greater flow-by area provided by a slim-style anchor. A recent independent computational fluid dynamics (CFD) research study compared a 5.5-in. standard B2 anchor with the new slim-style prototype TAC of the same size.

The study used CFD to compare gas flow within the annular space around two different types of a 5.5-in. tubing anchor catcher. Among the key findings were that the standard B2 TAC demonstrated a significantly higher level of kinetic turbulence and vorticity compared with the slim TAC. This turbulent flow, which can trap formation gas and lead to deposits of scale, paraffin and iron sulfide, is largely the result of the reduced flow‑by area of the standard B2 TAC vs. the slim‑style alternative.

According to the report, Fig. 1 illustrates how the “observed abrupt changes in the pressure field along with the potential presence of flow field obstacles in the case of the standard TAC is expected to generate more turbulence within the flow field along the TAC in comparison with the [slim-style] TAC.”

Fig. 1—Turbulence fields behavior between the traditional system and the new prototype. Source: TechTAC.
Fig. 1—Turbulence fields behavior between the traditional system and the new prototype.
Source: TechTAC.

The report also noted that “the vorticity strength in the flow field of the standard TAC is expected to be significantly present in comparison to that of the [slim-style TAC’s] case,” as illustrated in Fig. 2, which shows the vorticity field with strengths ranging between 0.0001 and 0.005.

Fig. 2—Computer illustration showing the vorticity fields behavior between the tools. Source: TechTAC.
Fig. 2—Computer illustration showing the vorticity fields behavior between the tools.
Source: TechTAC.

Conclusion

For wells struggling with persistent gas locking or scale issues that necessitate placing a TAC above the seat nipple, a new prototype slim TAC with a fullbore ID offers an alternative to conventional anchoring solutions. In the DJ Basin, one E&P operator adopted this slim-style TAC, enabling higher production from mature wells despite a high and rising GOR.

For Further Reading

DJ Basin Shifts to a Gassier Play, East Daley Analytics. (2025).

URTeC 1918491 Tubing Anchors Can Reduce Production Rates and Pump Fillage by J.N. McCoy, O.L. Rowlan, C.A. Taylor, and A.L. Podio.

Brad Crist is the president and owner of TechTAC, a tubing-anchor-solution provider that operates across several major US basins. Crist acquired the business in 2023 after more than 2 decades with critical materials management firm Savage Companies, where he held several leadership roles. He most recently served as president of the firm’s infrastructure sector, overseeing about 140 locations and 2,500 employees across the US, Canada, Mexico, and Saudi Arabia. His background includes managing operations at refineries, petrochemical plants, and transload facilities. Crist holds an MBA from the Wharton School of the University of Pennsylvania and a BA in economics from Brigham Young University.