Zephyr Energy 宣布 State 36-2R 井第二阶段生产测试成功

来源:www.gulfoilandgas.com 2024 年 9 月 6 日,地点:北美

Zephyr Energy plc 是一家专注于负责任的资源开发和碳中和运营的落基山石油和天然气公司,很高兴提供有关该公司位于美国犹他州 Paradox Basin 的旗舰项目 State 36-2R LNW-CC 井(“井”)运营的最新信息(“Paradox 项目”)。

该公司已完成该井生产测试的第二阶段(“第二次测试”),并于 2024 年 7 月 23 日宣布,并高兴地报告以下关键观察结果:

· 第二次测试期间实现的峰值产量超过每天 2,100 桶油当量(“boepd”),对于仅完成 130 英尺储层间隔的美国陆上油井来说,这是一个非常可观的产量。
· 酸化作业成功消除了任何剩余的近井筒地层损害并产生了非常高的储层产能,每次酸化处理后近井筒储层的渗透性都有显着改善。因此,该作业不仅消除了损害,还提高了储层生产力。
· 这是已知的第一个在 Paradox 盆地进行酸化刺激的例子,其结果对于该油田的开发非常有利,有可能大幅降低油藏风险,并且不再需要像在美国陆上其他资源油田中那样进行昂贵的水力刺激。

· 第二次测试中观察到了不同的液体产量,这些产量均高于该公司位于 Zephyr 的 Paradox 项目区域北部的 State 16-2 LN-CC 井(简称“State 16-2 井”)。在第二次测试的峰值生产率下,凝析油/轻质挥发油约占 510 桶油当量/天,并且这些液体产量在测试结束时呈上升趋势。o
液体产量的提高有可能成为改善经济效益的重要驱动因素,并可能增加整个公司 Paradox 项目区域的可采液体量。o
目前正在进行详细的流体实验室分析,结果将有助于公司进一步描述油田的流体填充和成分。
· 持续有证据表明水产量几乎为零,这又可能提高油井的经济效益,因为这样可以大大减少对昂贵的水处理的需求。

· 鉴于这些非常积极的观察结果,Zephyr 已开始与美国行业合作伙伴讨论潜在的油井和更广泛的 Paradox 项目开发机会,以期加快对 Paradox 项目的进一步评估和开发。

更多细节和后续步骤
除了清理任何剩余的地层损害外,酸化作业似乎还具有意想不到的好处,即显著提高了近井筒储层的质量(通过溶解储层中已知存在的方解石和白云石矿物,在这些矿物被溶解的地方产生更高的孔隙度和渗透性)。该公司此前已在 State 16-2 井和其他 Cane Creek 井的储层岩心内观察到广泛的小型裂缝。Zephyr 的初步分析表明,酸化可以显著提高整个储层基质的渗透性,包括小型裂缝(可能存在于公司的整个 Paradox 项目区域内)以及遇到的任何主要裂缝网络。

这意味着,与美国其他资源区使用的水力刺激作业相比,在较长的水平段使用酸化可能是一种具有成本效益的完井技术。与仅针对主要天然裂缝网络(Paradox 盆地这一部分的历史开发方法)相比,这种替代完井技术还可以为 Paradox 项目的长期开发提供更广泛、风险更低的方法。鉴于

对 Paradox 项目的积极影响,Zephyr 董事会(“董事会”)已立即启动流程,以确定行业或资产级金融合作伙伴,以加速进一步评估和油田开发。这可能以与行业运营商的合作、与非运营商投资者的合资企业或资产级融资的形式出现。董事会现在认为,钻探 State 16-2、State 36-2 和 State 36-2R 井所产生的数据,结合过去四年 Paradox 项目开发的重要技术分析(包括大量的 3D 地震、岩心样本、测井数据、刺激数据和最近的生产测试结果)为潜在合作伙伴提供了可靠的数据集以供评估。


现在,第二次测试已经完成,该井已按照标准操作暂时关闭,同时 Zephyr 的运营团队将评估新数据。一个关键的考虑因素是,是否在短期内生产该井,还是暂时推迟生产以延长井眼并提高整体碳氢化合物回收潜力。虽然该井目前能够实现相当大的生产率,但它只能从 130 英尺的完井间隔开始,这可能会导致井眼附近区域的枯竭,从而使得未来延长该井变得更加困难。

该井允许最多 10,000 英尺的横向延伸,并且任何未来的横向延伸都有望受益于更大的连通体积以及酸化对该油田高产能的重大积极影响。

此外,借助从​​第二次测试和公司其他 Paradox 井中获取的新数据,Zephyr 将尽快采取行动,制作一份更新的合格人员报告。

Zephyr 首席执行官 Colin Harrington 表示:
“这是公司在开发 White Sands Unit 及其更广泛的 Paradox 项目面积方面的一个重要里程碑。这是 Paradox 盆地首次使用酸化刺激,结果非常令人鼓舞 - 油井的产能和渗透率特别显著,导致峰值产量强劲。

通过大幅降低完井成本并增加高生产率的机会,而无需仅针对主要的天然裂缝带或部署成本更高的水力刺激,最新油井测试的结果可能对 Paradox 项目的未来价值产生重大积极影响。


“董事会目前正在考虑所有选择,包括从 State 36-2R 开采,以及通过延伸现有水平段大幅增加油井排水面积的可能性。在评估 Paradox 项目的下一步时,将考虑安全运营和资本效率。与此同时,鉴于这些非常积极的结果,我们已经开始与美国行业合作伙伴讨论资产层面的合作机会。

“总之,两次生产测试的结果大大提高了我们对 Paradox 盆地的了解,并开辟了一种非常有效的新开发替代方案。我们相信,这可能很有意义,因为我们寻求为股东释放巨大的额外价值。”

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原文链接/GulfOilandGas

Zephyr Energy announces successful result of State 36-2R well second phase production test

Source: www.gulfoilandgas.com 9/6/2024, Location: North America

Zephyr Energy plc the Rocky Mountain oil and gas company focused on responsible resource development and carbon-neutral operations, is pleased to provide an update on operations on the State 36-2R LNW-CC well (the "well") at the Company's flagship project in the Paradox Basin, Utah, U.S. (the "Paradox project").

The Company has completed the second phase of the production test on the well (the "second test"), as announced on 23 July 2024, and is pleased to report the following key observations:

· Peak production rates achieved during the second test were over 2,100 barrels of oil equivalent per day ("boepd"), a very significant production rate for an onshore U.S. well with only 130 feet of completed reservoir interval.
· The acidisation operation successfully removed any remaining near-wellbore formation damage and generated very high reservoir deliverability, with a notable improvement to near-wellbore reservoir permeability after each acid treatment. As such, the operation not only removed damage but also enhanced reservoir productivity.
· This is the first known example of acidisation stimulation in the Paradox Basin, and the result is highly positive for the development of the play, with the potential for substantially reduced reservoir risk and removal of the need for costly hydraulic stimulation as used in other U.S. onshore resource plays.

· Variable liquid-yields were observed over the second test, all of which are higher than that at the Company's State 16-2 LN-CC well (the "State 16-2 well") in the northern part of Zephyr's Paradox project acreage. At the peak production rates in the second test, condensate/light volatile oil represented approximately 510 boepd, and these liquid yields were on an increasing trend at the conclusion of the test.
o The elevated liquid yield has the potential to be a significant driver of improved economics and may increase recoverable liquid volumes across the Company's Paradox project acreage.
o A detailed fluid laboratory analysis is currently underway, and the results will help the Company further characterise the field's fluid fill and composition.
· Continued evidence of almost zero water production, another potential boost to the well's economics by material reducing the need for expensive water disposal.

· Given the highly positive observations, Zephyr has commenced the process of discussing potential well and wider Paradox Project development opportunities with U.S. based industry partners in an effort to accelerate additional appraisal and development of the Paradox project.

Additional detail and next steps
In addition to cleaning up any remaining formation damage, the acidisation operation appears to have had the unanticipated benefit of significantly enhancing near-wellbore reservoir quality (by dissolving calcite and dolomite minerals known to exist in the reservoir, creating higher porosity and permeability where those minerals have been dissolved away). The Company has previously observed widespread minor fracturing in the reservoir cores of the State 16-2 well and other Cane Creek wells. Zephyr's initial analysis suggests that acidisation could materially enhance the permeability of the overall reservoir matrix, including the minor fracturing (which may be present across the Company's entire Paradox project acreage position) as well as any major fracture networks encountered.

This implies that acidisation, when utilised across a longer lateral, may offer a cost-effective completion technique compared to the hydraulic stimulation operation used in other U.S. resource plays. This alternative completion technique could also offer a broader and lower risk method for the long-term development of the Paradox project versus solely targeting major natural fracture networks (the historical development approach in this part of the Paradox Basin).

Given the positive implications for the Paradox project, Zephyr's board of directors (the "Board") has launched an immediate process to identify an industry or asset-level financial partner to accelerate further appraisal and field wide development. This could come in the form of a farm-in with an industry operator, a joint venture with a non-operator investor, or asset level funding. The Board now believes that the data generated from drilling the State 16-2, State 36-2 and State 36-2R wells, combined with the significant technical analysis developed from the Paradox project over the past four years (including extensive 3D seismic, core samples, log data, stimulation data and the recent production test results) provides a robust dataset for prospective partners to evaluate.


Now that the second test has been completed, the well has been temporarily shut in as per standard operations while Zephyr's operations team evaluates the new data. A key consideration is whether to produce the well in the short term, or to defer production temporarily in order to extend the wellbore and increase overall hydrocarbon recovery potential. While the well is capable of considerable production rates in its current form, it would be doing so from only a 130-foot completed interval which could make it more difficult to extend the well in the future by causing depletion in the near well bore area.

The well is permitted for up to a 10,000-foot lateral extension, and any future lateral extension would be expected to benefit both from greater connected volumes and the material positive impact acidisation could have on the high deliverability of this play.

In addition, with the new data generated from the second test and that from the Company's other Paradox wells, Zephyr will move as quickly as possible to produce an updated Competent Persons Report.

Colin Harrington, Zephyr's Chief Executive, said:
"This is a highly significant milestone for the Company in its development of the White Sands Unit and its wider Paradox project acreage. This is the first known use of acidisation stimulation in the Paradox Basin and the results have been extremely encouraging - the well's deliverability and permeability are particularly notable, leading to the strong peak production rates witnessed.

By materially reducing completion costs and increasing chances of high productivity without having to target only major natural fracture zones or deploy higher cost hydraulic stimulation, the results from the latest well test could have significant positive implications for the future value of the Paradox project.


"The Board is now considering all options, including producing from the State 36-2R and the potential to materially increase the drained area of the well via the extension of the current lateral. Safe operations and capital efficiency will be taken into consideration when evaluating the next steps for the Paradox project. In parallel, and given these highly positive results, we have commenced discussions around asset-level partnership opportunities with U.S.-based industry partners.

"In all, the findings from the two production tests have considerably advanced our understanding of the Paradox Basin and have opened up a highly effective new development alternative. We believe this could be meaningful as we seek to unlock significant additional value for our shareholders."

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