Petro Matad 提供运营更新

来源:www.gulfoilandgas.com 2024 年 11 月 14 日,地点:亚洲

蒙古石油公司 Petro Matad Limited 是 AIM 上市的一家公司,该公司提供了以下有关 Heron-1 井生产运营以及其位于蒙古东部的 XX 区块生产分成合同区域的 Heron-2 井测试结果的最新信息。

要点
· Heron-1 井正在生产,其最大产能估计与 2019 年钻杆测试中实现的 821 桶/天相似或更高。
· 石油伴生气比预期的多,这提高了流动潜力,但也导致地面压力波动,因此目前的产量被限制在 200 至 300 桶/天的范围内。
· 产出的产品正在用卡车运往邻近的 XIX 区块 TA-1 设施并储存起来。与 XIX 区块运营商的合作协议的商业条款已经达成一致,最终措辞正在准备中,供 MRPAM 签署。一旦获得批准,就可以准备 XX 区块原油的出口文件,然后开始销售。
· Heron-2 已进行刺激和测试,石油与刺激液一起以低流量回收。该井正在暂停,刺激和压力数据将接受审查,以确定后续计划。

Heron-1 产量
如前所述,Heron-1 井于 10 月 24 日投产,并在自然流动下继续向地面生产石油,无需泵送。该井生产的伴生气量和压力高于盆地通常观察到的水平,这为该井提供了较高的初始流动潜力。速率测试已实现与 2019 年井测试作业期间记录的最大 821 桶石油/天 (bopd) 速率相似的流量,在某些测试中甚至高于该速率。鉴于地面观察到的高压,正在仔细监测流量,以确保套管和生产油管压力保持在安全公差范围内,目前产量被限制在 200 至 300 桶/天的范围内。虽然这符合我们在生产前对初始稳定产量的期望,但我们正在审查该油井以更高产量持续生产的潜力迹象,以确定是否可以对地面进行改造以提高稳定流量。

定期向第 19 区块的 TA-1 生产设施输送石油的工作正在进行中。同时,所有商业条款现已达成一致,合作协议的最终措辞正在准备中,其中包括有关如何卸载、测量和确认所生产石油量的细节。一旦与第 19 区块运营商达成一致,合作协议将提交给行业监管机构蒙古矿产资源和石油管理局 (MRPAM) 批准。公司正在努力加快这些最后步骤,之后将准备出口文件并开始向中国买家销售第 XX 区块的石油。与此同时,第 19 区块拥有大量存储容量,因此第 XX 区块的生产可以不间断地继续进行。Heron

-2 测试
Heron-2 井测试作业于 10 月 25 日在完成刺激计划后开始。随后,测试台出现重大发动机故障,损失了七天时间,但维修完成并恢复了运营。测试结束时,该井产出了一种混合油和被认为是增产液的物质,估计生产潜力约为 30 桶/天。这比 Heron-1 的观测速率要低得多,尽管它与盆地中其他一些井报告的流量一致。将审查测试期间记录的压力数据和增产作业的细节,以确定流量是否表明储层渗透性低或其他井下问题。Heron-2 现已暂停,一旦数据评估完成,将确定该井的后续计划。

Petro Matad 首席执行官 Mike Buck 表示:
“我们对 Heron-1 油井迄今为止的表现非常满意,我们很高兴看到其可能实现高于预期的稳定流速。我们正在紧急研究这个问题,但如果需要进行表面改造,则可能需要等到冬季停产后才能进行。向第 19 区块转移生产正在成为常态,我们正在努力尽快出口和销售第 20 区块原油。鉴于

Heron-1 油井生产的热情,Heron-2 油井测试尚未达到我们所希望的流速,但石油的存在和采收令人鼓舞,我们还需要做一些工作来了解目前的结果并确定油井的未来计划。这项工作将在未来几个月内完成,届时我们将最终确定 2025 年的运营计划。”


我们将适时提供进一步的运营更新。

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原文链接/GulfOilandGas

Petro Matad Provides Operational Update

Source: www.gulfoilandgas.com 11/14/2024, Location: Asia

Petro Matad Limited the AIM quoted Mongolian oil company, provides the following update on production operations at the Heron-1 well and the well test results from Heron-2 in its Block XX Production Sharing Contract area in eastern Mongolia.

Highlights
· Heron-1 is producing well with maximum deliverability estimated to be similar to or greater than the 821 bopd achieved on drill stem testing in 2019.
· The oil has more associated gas than expected which improves the flow potential but is also causing pressure fluctuations at surface and so production is currently choked back in the 200 to 300 bpd range.
· Production is being trucked to the neighbouring Block XIX TA-1 facilities and stored. The commercial terms of the Cooperation Agreement with Block XIX operator have been agreed and the final wording is being prepared for sign off by MRPAM. Once approved, export paperwork for Block XX crude can be prepared and sales will then commence.
· Heron-2 has been stimulated and tested with oil recovered together with stimulation fluid at a low flow rate. The well is being suspended and the stimulation and pressure data will be reviewed to determine the forward programme.

Heron-1 production
As previously reported, the Heron-1 well was brought onstream on 24 October and it continues to produce oil to surface under natural flow without the need for pumping. The well is producing with higher amounts of associated gas and at higher pressures than are generally observed in the basin giving the well high initial flow potential. Rate tests have achieved flow rates similar to, and in some tests, higher than the maximum 821 barrels of oil per day (bopd) rate recorded during the well testing operations in 2019. Given the high pressures observed at surface, the flow rate is being monitored carefully to ensure that casing and production tubing pressures remain within safety tolerances and production is currently choked back to a range between 200 and 300 bpd. Whilst this is in line with our pre-production aspiration for an initial stabilised rate, the indications of sustained potential for the well to produce at higher rates are under review, to see if modifications at surface can be made to increase the stabilised flow rate.

Regular transfer of oil to the TA-1 production facilities in Block XIX is ongoing. Meanwhile, all the commercial terms have now been agreed and the final wording of the Cooperation Agreement is being prepared to include details of exactly how the produced volumes will be offloaded, measured and confirmed by the relevant parties. Once agreed with the Block XIX operator the Cooperation Agreement will be presented to the industry regulator, the Mineral Resources and Petroleum Authority of Mongolia (MRPAM) for their approval. The Company is pushing to expedite these final steps after which export paperwork will be prepared and sales of Block XX oil to the buyer in China will commence. In the meantime, large storage capacity is available in Block XIX so Block XX production can continue uninterrupted.

Heron-2 testing
Heron-2 well testing operations commenced on 25 October following completion of a stimulation programme. Seven days were subsequently lost after the test rig suffered a major engine problem but repairs were completed and operations resumed. By end of the test, the well was producing a mixture of oil and what is interpreted to be stimulation fluids with productive potential estimated to be around 30 bpd. This is significantly lower than the rates observed in Heron-1 although it is in line with flow rates reported from some other wells in the basin. Pressure data recorded during the test and the details of the stimulation operation will be reviewed to determine if the flow rate is an indication of low reservoir permeability or some other down-hole issue. Heron-2 is now being suspended and once the data evaluation is complete, the forward programme for the well will be determined.

Mike Buck, CEO of Petro Matad, said:
"We are very pleased with the performance of the Heron-1 well so far and we are encouraged that higher than expected stabilised flow rates may be achievable. We are looking into this as a matter of some urgency, although if surface modifications are needed, these will likely have to wait until after the winter operational shut down. The transfer of production to Block XIX is settling into a routine and we are pushing to be able to export and sell Block XX crude as soon as possible.

The Heron-2 well testing has not achieved the flow rates we were hoping for given the enthusiasm with which Heron-1 produces, but the presence and recovery of oil is encouraging and we have some work ahead to understand the outcome so far and determine the forward programme for the well. This work will be done over the next few months as we finalise our operational programme for 2025."


Further operational updates will be provided in due course.

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