58 区块的 Kunooz-1 勘探井已钻至最终深度

来源:www.gulfoilandgas.com 2024 年 10 月 29 日,地点:中东

阿曼苏丹国陆上 58 号区块的 Kunooz-1 勘探井已钻至最终深度 3,923 米。两个目标地层的电缆测井作业已完成。测井结果表明,该地层的孔隙度低且有裂缝,需要进行流动测试以确认可能存在碳氢化合物。进一步的完井和流动测试预计将持续约四周。

垂直 Kunooz-1 勘探井的钻井作业已完成。该井以 Buah 和 Khufai 地层为主要目标,以 Birba 地层为次要目标,最终总深度为 3,923 米。Birba

和 Buah 地层的电缆测井结果表明,该地层的裂缝性白云质灰岩总厚度约为 500 米,基质孔隙度低。储层部分钻井液全部漏失,没有岩屑流出地面。这表明储层渗透性高,但为随钻评估碳氢化合物潜力提供了有限的数据。需要进行流动测试以确认 Birba 和 Buah 地层中可能存在的碳氢化合物潜力。由于操作方面的挑战,没有从较深的 Khufai 地层收集到足够的数据。

将开始进一步的完井和测试以评估井的流动性能。井测试计划包括 Birba 和 Buah 地层的裸眼完井,以及对收集的数据进行进一步分析。井测试计划预计将在大约四周内完成。

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原文链接/GulfOilandGas

The Kunooz-1 Exploration Well on Block 58 Drilled to its Final Depth

Source: www.gulfoilandgas.com 10/29/2024, Location: Middle East

The exploration well Kunooz-1 on Block 58 onshore Sultanate of Oman has drilled to its final depth of 3,923 metres. Wireline logging operations have been completed for two of the target formations. The logs indicated low porosity and fractured dolomitic limestone that will require a flow test to confirm a possible hydrocarbon potential. Further well completion and flow testing is expected to be ongoing for approximately four weeks.

The drilling operations of the vertical Kunooz-1 exploration well have been completed. The well targeted the Buah and Khufai formations as its primary targets with the Birba formation as its secondary target and had a final total depth of 3,923 metres.

Wireline logging of the Birba and Buah formations indicated an approximately 500 metres gross thickness of fractured dolomitic limestone and low matrix porosity. The reservoir section was drilled with total drilling fluid losses with no cuttings to surface. It indicates high reservoir permeability but provided limited data availability for while-drilling evaluation of hydrocarbon potential. A flow test is required to confirm a possible hydrocarbon potential in the Birba and Buah formations. No sufficient data was collected from the deeper Khufai formation due to operational challenges.

Further well completion and testing will commence to evaluate the well’s flow performance. The well testing programme includes an open hole completion of the Birba and Buah formations, alongside further analysis of collected data. The well testing programme is expected to be completed in approximately four weeks.

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