成熟田

玻利维亚的成功案例:雷普索尔公司如何治理安第斯山麓一口油井的结垢问题

运营商开发出一种解决方案,使油井在处理后一年多来保持稳定生产。

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雷普索尔公司位于玻利维亚南部安第斯山脉以南W油田的W8井遭遇了结垢问题。作业者介入解决该井的结垢问题后,其恢复生产的时间很短。最终,作业者采用了一套综合解决方案,实现了超过一年的稳定生产。图中所示为W8井滑动侧门的井下摄像机图像,(a)为有机酸酸洗处理前,(b)为有机酸酸洗处理后。
来源:SPE 227964。

在玻利维亚南部安第斯山脉以南的一口油井中,经过 15 年的生产,首次出现结垢导致天然气产量下降的情况,原因是完井层与水不相容,这促使人们采取了多次干预措施。 

几次有机酸洗作业溶解了水垢,使油井暂时恢复生产,但这并非长久之计。通过对水垢成分和来源的评估,油井生产团队制定了一项修复方案,最终使油井恢复生产,并将清理间隔从不到3个月延长至一年以上。

雷普索尔公司高级油藏工程师亚历杭德罗·古兹曼在10月份举行的SPE年度技术会议暨展览会(ATCE)上发表SPE 227964号报告时表示,该油井结垢问题的解决方案包括油管酸洗、区域隔离、近井筒酸洗和阻垢剂处理。他表示,这些措施使团队能够将日产量从1900万立方英尺提升至7500万立方英尺,并保持了一年多的稳定产量。

位于安第斯山麓盆地南部W油田的W8井,储层岩石为石英砂岩,孔隙度为4%。他表示,该井虽然成本高昂,但潜力巨大。该井总深度约6000米,最大斜井角度为27°,共有三个产气层,其中上部和中部产气层此前已为人所知,而下部产气层则是新发现的。虽然下部产气层此前被认为是独立的,但井测试表明,下部产气层存在向上方产气层的串流,而上方产气层也由附近的井生产。 

W8井投产不到3个月,产量就从7000万立方英尺/天骤降至3000万立方英尺/天。古兹曼表示,团队最初将井口压力下降归因于机械故障。但经电缆摄像(图1)证实,井底深处存在严重结垢,这在该油田历史上尚属首次。

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图 1——确定 W8 井油管结垢的事件顺序为:(a)从下部到上部的横向流动;(b)气体产量(MMcf/D)和井口压力(WHP)性能下降;(c)使用钢丝绳测径器识别通道阻塞;(d)使用电缆摄像机确认结垢。 
来源:SPE 227964。

对W8井结垢样品进行现场实验室分析后,生产团队决定采用一种有机酸浸渍混合物,该混合物在实验室和实际应用中均有效。油管处理后,油井恢复生产,但产量很快再次下降。随后进行了另一次干预,但结果类似(图2)

古兹曼说,这两项工作“都实现了结垢和恢复生产的立即交付,但生产稳定性持续不到3个月”。

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图 2—井 W8 的天然气产量(MMcf/D)和井口压力(WHP)性能。
来源:SPE 227964。

为了解决油井的长期问题,生产团队采用了多步骤工作流程,分析流体和结垢,测试结垢对酸处理的溶解度,分析系统流体的兼容性,分析岩石流体,并创建结垢的综合模型。 

水质分析表明,上层水体受到下层水体横向流动的影响,两层水体的产出水成分非常相似。实验室测试了该水体的结垢情况,结果表明,在 80°F 和 200°F 的温度下,样品在第三天开始出现沉淀,且高温下结垢更为严重。

矿物学分析表明,该样品完全由方解石沉淀物组成。氧化皮分析显示,在暴露于由13%乙酸和9%甲酸组成的有机酸中1小时内,78%的样品溶解;接触4小时后,98%的样品溶解。

随后对系统流体(油藏产出的冷凝水和水)与有机酸以及粘土、腐蚀和结垢抑制剂的相容性进行了分析。作者指出,在200°F(93°C)下接触48小时后,油藏流体和处理流体之间未观察到乳化或沉淀现象。

研究团队测试了添加不同浓度的聚丙烯酸酯基阻垢剂的效果,发现它可以有效防止结垢,而无需添加其他添加剂。

岩石流体相容性分析表明,在井筒附近用酸处理是可行的,而不仅仅局限于对油管进行酸洗,作者表示,酸洗最终能提供更深层的清洁效果。

研究团队还确定了水垢的来源。他们利用市售的水垢分析软件对系统进行建模,从而确定了运行条件、可生产区域以及最佳气体流量。研究发现,压力下降和流通面积变化,以及温度、pH值、钙和碳酸盐浓度的升高,都会导致水垢的形成。生产滑动套筒处的压力下降会导致水垢形成,而最容易积聚水垢的位置是上下两区混合点。水的不相容性也会增加水垢形成的倾向。

古兹曼表示,制作团队已获准根据多步骤工作流程进行干预。

此次干预措施包括用酸液浸泡油管、环空和储层上表面7小时,井测试验证了W8井的生产情况。同时安装了电塞,以隔离中间层,防止水不相容性导致未来结垢。注入阻垢剂并浸泡5小时后,再次进行生产测试,之后将油井重新接入生产集输系统。

他表示,产量立即从 19 MMcf/D 恢复到 75 MMcf/D,然后稳定在 66 MMcf/D 的持续水平(图 3)

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图 3—井 W8 天然气产量(MMcf/D)和井口压力(WHP)历史。
来源:SPE 227964。

古兹曼表示,此次生产“与以往不同”,因为使用阻垢剂后,该井的日产量维持在 6600 万立方英尺,持续了一年多。

他将此次干预的成功归功于旨在解决水体不相容性、现有流量限制和防止未来结垢的综合解决方案。

“这口井的情况比以前好多了,”他说。

此外,作者指出,该方法已应用于更广泛的钨领域,并确定了未来化学处理的候选对象。

延伸阅读

SPE 227964 一种有效的阻垢剂和定制的酸洗成功地在成熟产气田严重结垢后维持了油井产能:安第斯山脉南部油田的案例研究,作者: A. Guzmán,Repsol;S. Alvarado,Repsol Oil & Gas USA;C. Barbery,Repsol SA;M. Morón 和 H. Antelo Otterburg,Repsol;C. Miranda,Repsol E&P Bolivia;L. Antelo,Halliburton Co.;以及 C. Paz,Halliburton。

原文链接/JPT
Mature fields

Bolivian Success: How Repsol Remediated Scale in a Sub-Andean Well

The operator developed a solution that has kept the well at stable production for over a year after treatment.

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Repsol faced scale issues at its W8 well in the W field in Sub-Andean southern Bolivia. After the operator intervened to resolve scale issues at this well, its return to productivity was short-lived. The operator ultimately used a comprehensive solution that resulted in stable production for more than a year. Seen here are downhole video camera images of the Well W8 sliding side door (a) before organic acid pickling, and (b) after organic acid pickling.
Source: SPE 227964.

Scale choked gas output for the first time in a Sub-Andean, south Bolivian well after 15 years of production because of water incompatibility between completed zones, prompting several interventions. 

A couple of organic acid pickling jobs dissolved the scale and brought the well temporarily back online, but they didn’t provide a long-term solution. An assessment of the composition and origin of the scale led the well’s production team to identify a remediation plan that ultimately returned the well to production and increased the time between cleanup interventions from less than 3 months to over a year.

Alejandro Guzmán, senior reservoir engineer at Repsol, said while presenting SPE 227964 at SPE’s Annual Technical Conference and Exhibition (ATCE) in October that the solution for the well’s scale problems involved tubing acid pickling, zonal isolation, near-wellbore acid, and scale inhibitor. These efforts enabled the team to bring production levels from 19 MMcf/D up to 75 MMcf/D with prolonged stability of more than a year, he said.

Well W8, located in the W field in the southern Sub-Andean basin, produces from quartzite sandstone reservoir rock with 4% porosity. The well had been high-cost but also had high potential, he said. With a total depth of about 6,000 m and a maximum deviation of 27°, it had three gas-producing zones, of which the upper and middle zones were previously known, while the lower zone was a new encounter. While the lower zone was isolated, well testing revealed crossflow from the lower zone to the upper zone, which was also being produced by nearby wells. 

Well W8 suffered an abrupt flow-rate decrease, from 70 MMcf/D to 30 MMcf/D less than 3 months after being put online. Guzmán said the team initially ascribed the decrease in wellhead pressure to a mechanical problem. A restriction at depth was found to be severe scale for the first time in the field’s history, confirmed by wireline video camera (Fig. 1).

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Fig. 1—The sequence of events to determine scale in well W8 tubing was (a) crossflow from lower to upper zone, (b) declining performance of gas rate (MMcf/D) and wellhead pressure (WHP), (c) identification of passage restriction with slickline gauge cutter, and (d) confirmation of scale using wireline video camera. 
Source: SPE 227964.

Analysis in an in-situ lab of a scale sample from Well W8 prompted the production team to use an organic acid pickling blend that was effective in the lab and at scale. Post-tubing treatment, the well went back online, but soon production dropped again. Another intervention followed, but with similar results (Fig. 2).

Both jobs “resulted in scale dissolution and immediate delivery of recovered production, but production stability lasted less than 3 months,” Guzmán said.

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Fig. 2—Well W8 gas-rate (MMcf/D) and wellhead-pressure (WHP) performance.
Source: SPE 227964.

Needing a long-term solution for the well, the production team turned to a multistep workflow to analyze the fluids and scale, test the scale solubility in response to acid treatment, analyze the system fluids compatibility, analyze rock fluids, and create an integrated model of the scale. 

The water analysis showed the upper-zone water was influenced by crossflow water from the lower zone, with produced water from both zones being very similar. Scale formation from this water was tested in the lab, with precipitates forming from the third day in samples at 80°F and 200°F, with more severe scale at the higher temperature.

Mineralogy analysis indicated the sample was exclusively calcite precipitate. Scale analysis revealed that within 1 hour of exposure to an organic acid composed of 13% acetic acid and 9% formic acid, 78% of the sample had dissolved, and 98% had dissolved within 4 hours of contact.

A compatibility analysis of systems fluids—condensate and water produced from the reservoir—with organic acid and inhibitors for clay, corrosion, and scale followed. No emulsions or precipitates between reservoir and treatment fluids were observed after 48 hours of contact at 200°F, according to the authors.

The team tested the addition of a polyacrylate-based scale inhibitor at different concentrations and found it could be used effectively to prevent scaling without needing further additives.

The rock-fluids compatibility analysis indicated the feasibility of treating with acid near the wellbore rather than being restricted to applying acid pickling to the tubing, which the authors said ultimately provided a deeper cleaning effect.

The team also determined the origin of the scale. They modeled the system with commercially available scale-analysis software, which allowed them to define operating conditions, zones open to production, and optimum gas rate, according to the paper. They found that pressure decrease and flow-area changes, combined with increases in temperature, pH, and calcium and carbonate concentrations, contributed to scale forming. Decreased pressure at the production sliding sleeves led to scale formation, and the most likely location for scale buildup is the production mixing point of the upper and lower zones. Water incompatibility increased the tendency for scale formation.

The production team got the green light to carry out an intervention informed by the multistep workflow, Guzmán said.

The intervention soaked the tubing, as well as the annulus and upper reservoir face, with acid for 7 hours, and well testing verified production at Well W8. Electric plugs were also installed to isolate the intermediate zone and avoid water incompatibility from causing scale to form in the future. The scale inhibitor was pumped and allowed to soak for 5 hours, followed by another production test before the well was tied back into the production-gathering system.

Production immediately recovered from 19 MMcf/D to 75 MMcf/D before settling at a sustained level of 66 MMcf/D, he said (Fig 3).

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Fig. 3—Well W8 gas-rate (MMcf/D) and wellhead-pressure (WHP) history.
Source: SPE 227964.

The production “was different from the past” in that the application of the scale inhibitor allowed the well to maintain production at 66 MMcf/D for more than a year, Guzmán said.

He attributed the success of this intervention to the comprehensive solution designed to address water incompatibility, the existing flow restriction, and the prevention of future scale.

“The well is behaving better than before,” he said.

Further, the authors noted that the methodology has been applied across the wider W field and has identified candidates for future chemical treatment.

For Further Reading

SPE 227964 An Effective Scale Inhibitor and a Tailored Acid Cleanout Successfully Maintains Well Productivity After Severe Scale Formation in a Mature Gas-Producing Field: Case History in a Sub-Andean South Field by A. Guzmán, Repsol; S. Alvarado, Repsol Oil & Gas USA; C. Barbery, Repsol S.A.; M. Morón and H. Antelo Otterburg, Repsol; C. Miranda, Repsol E&P Bolivia; L. Antelo, Halliburton Co.; and C. Paz, Halliburton.