TMK 宣布 2024 年 12 月运营评估

来源:www.gulfoilandgas.com 2025 年 1 月 2 日,地点:亚洲

? 2024 年 12 月,试验生产井和设施的正常运行时间接近 100%
? 恢复正常泵速后,原三口试验井(LF-01、LF-02 和 LF-03)的天然气生产迅速恢复
? 新井(LF-04、LF-05 和 LF-06)的液位正在缓慢降低,产水量强劲,表明渗透性良好
? 分布式温度传感 (DTS) 数据已成功收集,随着获得更多数据,将在未来几个月内对其进行解释

TMK Energy Limited(“TMK”或“公司”)很高兴地报告,所有六口试验生产井,包括 Gurvantes XXXV 煤层气 (CSG) 项目最近钻探的三口试验生产井,自投入使用之日起在 2024 年 12 月全月成功生产,仅因第三方轻微断电而导致的极短停机时间。

在钻探新的试验井时,三口原试验井(LF-01、LF-02 和 LF-03)的泵速处于空转状态,使气体流量几乎降至零。新井投入使用后,原井的泵速逐渐提高,一旦液位降至先前水平,气体流量就会迅速恢复到这些井中。新井

(LF-04、LF-05 和 LF-06)中的液位继续按照油藏管理计划缓慢下降。液位已降低约 30% 至所需水平,并将在未来 2-3 周内继续降低,届时所有六口井都将达到其设计液位。


成功从 LF-04 和 LF-05 收集了 DTS 数据,目前正在审查中。DTS 是一种重要工具,有助于确定非常厚的生产间隔内哪些区域贡献了最多的水和/或气体。随着这些井中的液位继续下降,未来几周将收集更多数据,然后预计在未来几个月内能够详细解释这些数据。TMK

Energy 首席执行官 Dougal Ferguson 先生评论道:
“我们很高兴地报告,这些井和设施在整个 2024 年 12 月都运行得非常高效,而且这些井的表现符合预期。

很高兴看到原始井的天然气产量迅速恢复到与以前相同甚至略高的水平。一旦新井在未来几周内达到其设计流体水平,我们预计将看到这些井产气,并在达到大幅增加气体流量所需的临界解吸压力方面取得实际进展。”

根据澳大利亚证券交易所上市规则 15.5 的规定,董事会已授权发布此公告。

测井、射孔、测试 >>

蒙古测井、射孔、测试新闻 >>



美国 >> 2024 年 12 月 31 日 - 88 Energy Limited (ASX:88E、AIM:88E、OTC:EEENF)(88 Energy、88E 或公司)很高兴提供有关 Project Phoenix 合资公司的最新信息......
巴基斯坦 >> 2024 年 12 月 24 日 ——石油天然气开发有限公司 (OGDCL) 欣然宣布成功恢复达尔西 2 号井,实现了碳氢化合物生产……

印度 >> 2024 年 12 月 19 日 - Synergia Energy Limited(“Synergia”或“公司”)董事会宣布对公司在印度的 Cambay PSC(WI:50%)进行以下更新

。...

巴基斯坦 >> 2024 年 12 月 19 日 ——我们很高兴地宣布,Kunnar West Well-3 已成功投入生产,井口流压 (WHFP) 为 1200 PSI……




原文链接/GulfOilandGas

TMK Announces Operations Review - December 2024

Source: www.gulfoilandgas.com 1/2/2025, Location: Asia

? Pilot Production wells and facilities operated close to 100% uptime during December 2024
? Gas production from original three pilot wells (LF-01. LF-02 and LF-03) quickly resumed following return to normal pump speeds
? Fluid levels being slowly reduced in new wells (LF-04, LF-05 and LF-06) with strong water production indicating good permeability
? Distributed Temperature Sensing (DTS) data being successfully collected and to be interpreted in the coming months as more data acquired

TMK Energy Limited (TMK or the Company) is pleased to report that all six pilot production wells, including the three recently drilled pilot production wells at the Gurvantes XXXV Coal Seam Gas (CSG) Project, have been successfully producing from the date of commissioning for the full month of December 2024, with only minimal downtime due to minor third-party power outages.

The pump speeds on the three original pilot wells (LF-01, LF-02 and LF-03) were run at idle speed during the drilling of the new pilot wells, reducing gas flows to almost zero. Following commissioning of the new wells, the pump speeds of the original wells were gradually increased and gas flows quickly returned to these wells once fluid levels were reduced to prior levels.

Fluid levels in the new wells (LF-04, LF-05 and LF-06) continue to be drawn down slowly in accordance with the reservoir management plan. Fluid levels have been reduced by approximately 30% towards the desired level and will continue to be reduced over the next 2-3 weeks, at which point all six wells will be at their design fluid levels.


DTS data is successfully being collected from LF-04 and LF-05 and is currently being reviewed. The DTS is an important tool to help identify which zones within the very thick production interval are contributing the most water and/or gas. Further data will be collected in the coming weeks as fluid levels continue to decrease in these wells, with the data then expected to be able to be interpreted in detail in the coming months.

Mr Dougal Ferguson, TMK Energy’s Chief Executive Officer commented:
“We are pleased to report that the wells and facilities have operated very efficiently throughout the month of December 2024 and the wells are performing in line with expectations.

It is pleasing to see the gas production from the original wells quickly return at the same, if not slightly better rates than before. Once the new wells reach their design fluid levels in the next few weeks, we expect to see gas production from those wells and start making real progress towards reaching the critical desorption pressures required for a material increase in gas flow rates.”

For the purposes of ASX Listing Rule 15.5, the Board has authorised for this announcement to be released.

Logging, Perforating, Testing >>

Logging, Perforating, Testing News in Mongolia >>



United States >>  12/31/2024 - 88 Energy Limited (ASX:88E, AIM:88E, OTC:EEENF) (88 Energy, 88E, or the Company) is pleased to provide an update on Project Phoenix’s joint venture pa...
Pakistan >>  12/24/2024 - Oil & Gas Development Company Limited (OGDCL) is pleased to announce the successful revival of Dars West-2 Well, achieving hydrocarbon production from...

India >>  12/19/2024 - The Board of Synergia Energy Limited (Synergia or the Company) announces the following update to the Company's Cambay PSC (WI: 50%) in India.

...

Pakistan >>  12/19/2024 - We are pleased to announce that Kunnar West Well-3 has been successfully brought into production at a wellhead flowing pressure (WHFP) of 1200 PSI wit...