使用移动流入剖面监测完井的现场经验

西夫科姆内夫特天然气有限责任公司

P. Likhachev ― LikhachevPA@skn.rosneft.ru

B. 库赛诺夫BI_Khusainov@skn.rosneft.ru

P. Leontiev — PV_Leontev2@skn.rosneft.ru

虫洞研发有限责任公司

O. Zhuravlev Øzhuravlev@wormholes.ru

A.格里巴诺夫“ agribanov@wormholes.ru”

A. 苏沃洛夫 — asuvorov@wormholes.ru

油气田开发的效率很大程度上取决于碳氢化合物生产相关成本的多少。当前的行业趋势表明,成功的公司是那些积极实施旨在降低生产成本和提高生产流程效率的技术解决方案的公司。在竞争激烈的环境下,技术现代化不再是一种额外的优势,而是可持续发展和市场稳定的必要条件。

近几十年来钻井领域最显著的成就之一是水平井的广泛应用,这使得油藏采收率显著提高。然而,生产井筒长度的增加也带来了新的挑战,主要是需要对井筒沿线的流体相分布进行详细可靠的监测。传统地球物理方法,尤其是基于连续油管或井下牵引装置的系统,存在诸多局限性。这些局限性包括:水力损失高、自然流入量畸变、下潜深度有限以及作业过程中出现并发症的可能性高。

为了应对这些挑战,SevKomNefteGaz实施并测试了一套基于标记技术的可重复使用回收系统。该系统的应用使得能够在不干扰油井作业模式的情况下,获取沿水平井筒流入量分布的定量特征。这不仅节省了时间和财务成本,还提高了产能预测的准确性,这直接影响着油田的进一步开发策略。

与WORMHOLES研发公司合作,在北共青团油田实施了一个可回收标记系统(见图1)的运行项目。该系统基于此前已在一百多口井中实施的解决方案,可在生产层的不同层段安装监测模块。这使得能够构建详细的流入剖面图,并识别油水流入区域,从而为后续开发方案的调整提供依据。

图1. 间隔流入监测装置

该系统的运行通过使用与油或水接触后发生反应的活性标记物来确保。这些成分会释放示踪剂,这些示踪剂可在采集的样品中检测到。通过在井口对地层流体进行连续采样,并随后进行实验室分析,可以准确评估各个区域对总产量的贡献,而无需中断既定的设备运行模式。这种方法消除了传统方法中常见的数据失真,使监测更加可靠且经济合理。

作为试点项目的一部分,这项工作分两个阶段进行。第一阶段,在井的水平段部署了带有标记盒的组件。第二阶段包括在井口进行系统采样,并在WORMHOLES研发中心的实验室对样品进行分析。采样工作在井达到投产状态后进行。

在其中一口水平井中,应用了一种改进的分布式流入剖面监测标记系统。该设备安装在直径73毫米的油管上,并固定在直径114毫米的生产井水平段。该井设计包含15个封隔器,形成8个生产层段。为了对流入剖面进行当前的分析,使用了监测模块,这些模块均匀分布在4个关键层段上,每个层段覆盖多个流入区域。部署到计划深度后,使用标准液压断开器断开该组件。

实施过程中遇到的关键工程挑战之一是设备极易淤积,这与油井生产中存在磨蚀性夹杂物有关。该组件在井筒水平段的延伸配置也带来了额外的风险,尤其是在长时间不回收作业的情况下。这证明了在新版系统中放弃使用封隔器的决定是合理的。改进后的组件可在油管和尾管之间的环形空间内实现流体循环,同时通过在底部安装盲靴来防止流体进入油管内部。流体从井底流向井口,从而可以单独标记每个层段。为了稳定流体动力学,测量模块中集成了额外的湍流生成元件。

安装完成后,在井中安装了一台电动潜水泵,并投入运行。产量稳定一周后,开始井口取样——连续五天,每天采集两次流体样品,送往实验室分析,以确定标记物浓度。

实施方法的主要优点包括:

  • 降低技术风险:取消封隔器,采用循环方案,确保稳定运行,无堵塞。

  • 提高监测可靠性:标记可以确定油和水的定量流入量。

  • 操作模式的维护:连续采样无需停井,保持自然的操作条件。

  • 灵活性和适应性:调整采样计划可以解释流入的动态并提高解释的准确性。

该系统在矿化程度高、机械杂质含量高的条件下表现出了良好的效果。其与现有基础设施(尤其是73毫米油管和电潜泵)的兼容性,证明了其在成熟油田和水淹油田的适用性。所获取的数据为后续地质和技术分析以及堵水方案的制定奠定了基础。

图 2. 间隔流入量剖面图,m鲁/天

图 3. 区间水流入量,%

图 4. 区间油流入量,%

实验室研究(图 2、3 和 4)表明剖面具有明显的非均匀性:在井底段,主要流入水量为 57.7 立方米/天水和 34.9 立方米/天油,占总流量的近 60%;而在井口,流入水量为 21.5 立方米/天水和 6.0 立方米/天油。

隔离模型揭示了以下情况:

  • 隔离下部层段使含水率降低了 2.5%,但同时损失了 66.2 立方米/天的石油。

  • 井口隔离使含水率降低了 3.9%,石油损失量为 32.9 立方米/天。

  • 通过对上下层段进行综合封隔及下部出砂堵漏,总含水率降低16.1%,但总产量下降:液量减少120.2立方米/天,油量减少70.6立方米/天。

这些结果强调了采取战略性含水管理方法的必要性,不仅要注重减少水流入量,还要维持可接受的石油产量水平。因此,从含水量降低与石油损失的比率来看,隔离4号层段的方案被证明是更可取的。

监测完成后,该组件已按照批准的方案成功回收。检查结果证实了所有部件的技术完整性,因此该设备可以重复使用,无需额外修复费用。

因此,该方法兼具技术创新性和实用价值,能够准确评估入流剖面,降低淤积风险,并可快速集成到现有技术流程中。该方法的应用有助于在含水率上升、地质和生产条件复杂化的情况下做出更明智的决策。

原文链接/RogtecMagazine

Field Experience of Using a Mobile Inflow Profile Monitoring Completion

SevKomNefteGaz LLC

P. Likhachev — LikhachevPA@skn.rosneft.ru

B. Khusainov — BI_Khusainov@skn.rosneft.ru

P. Leontiev — PV_Leontev2@skn.rosneft.ru

WORMHOLES R&D LLC

O. Zhuravlev — ozhuravlev@wormholes.ru

A. Gribanov — agribanov@wormholes.ru

A. Suvorov — asuvorov@wormholes.ru

The efficiency of developing oil and gas fields is largely determined by the magnitude of the costs associated with hydrocarbon production. Current industry trends indicate that the companies that succeed are those that actively implement technological solutions aimed at reducing production costs and increasing the efficiency of production processes. Under conditions of high competition, technological modernization is no longer an additional advantage — it has become a necessary condition for sustainable development and market stability.

One of the most significant achievements of recent decades in the field of drilling has been the widespread adoption of horizontal wells, which allow for a significant increase in reservoir recovery. However, the increase in the length of the productive borehole has led to the emergence of new challenges, primarily the need for detailed and reliable monitoring of the fluid phase distribution along the wellbore. The use of traditional geophysical methods, particularly systems based on coiled tubing or downhole tractor devices, is associated with several limitations. Among these are high hydraulic losses, distortion of the natural inflow, limited depth of descent, and a high probability of complications during operations.

As part of addressing these challenges, SevKomNefteGaz implemented and tested a reusable retrievable system based on marker technologies. The application of this system enabled the acquisition of quantitative characteristics of inflow distribution along the horizontal wellbore without interfering with the operating mode of the well. This not only reduced time and financial costs but also improved the accuracy of productivity forecasting, which directly influences the strategy for further field development.

In collaboration with WORMHOLES R&D, a project was carried out to operate the retrievable marker system (see Figure 1) at the Severo-Komsomolskoye field. The system, based on solutions previously implemented in more than a hundred wells, provides for the installation of monitoring modules at various intervals of the productive formation. This makes it possible to construct a detailed picture of the inflow profile and to identify zones of oil and water inflow, which allows for subsequent adjustments to the development regime.

Figure 1. Device for Interval Inflow Monitoring

The operation of the system is ensured through the use of active markers that react upon contact with oil or water. These components release tracers that are detected in the collected samples. Sequential sampling of formation fluid at the wellhead and its subsequent laboratory analysis make it possible to accurately assess the contribution of individual zones to the total production rate, without disrupting the established equipment operating mode. This approach eliminates the data distortion typical of traditional methods and makes monitoring more reliable and economically justified.

As part of the pilot project, the work was carried out in two stages. During the first stage, a deployment of the assembly with marker cassettes was performed in the horizontal section of the well. The second stage included systematic sampling at the wellhead and analysis of the samples at the laboratory of WORMHOLES R&D. Sampling was carried out after the well reached its operational mode.

An improved marker system for distributed inflow profile monitoring was applied to one of the horizontal wells. The equipment was installed on 73-mm diameter tubing and fixed in the horizontal section of the 114-mm diameter production well. The well design included fifteen packers, forming eight productive intervals. For the current analysis of the inflow profile, monitoring modules were used, evenly distributed across four key intervals, each covering several inflow zones. After deployment to the planned depth, the assembly was disconnected using a standard hydraulic disconnector.

One of the key engineering challenges encountered during implementation was the high likelihood of equipment silting, associated with the presence of abrasive inclusions in the well’s production. An additional risk was posed by the extended configuration of the assembly in the horizontal section of the wellbore, especially during prolonged operation without retrieval. This justified the decision to abandon the use of packers in the new version of the system. The modified assembly provided for fluid circulation in the annular space between the tubing and the tailpipe, while preventing fluid ingress inside the tubing through the installation of a blind shoe in the bottom part. The flow moved from the bottomhole to the wellhead, allowing each interval to be individually marked. To stabilize the hydrodynamics, additional turbulence-generating elements were integrated with the measuring modules.

After installation was completed, an electric submersible pump was installed in the well, and the facility was put into operational mode. After one week of stabilized production rate, wellhead sampling began — for five days, fluid samples were collected twice a day and sent for laboratory analysis to determine marker concentrations.

The key advantages of the implemented approach include:

  • Reduction of technological risks: the abandonment of packers and the circulation scheme ensured stable operation without blockage.

  • Improved monitoring reliability: the markers made it possible to determine the quantitative inflow of oil and water.

  • Maintenance of the operating mode: continuous sampling eliminated the need to shut down the well, preserving natural operating conditions.

  • Flexibility and adaptability: adjustment of the sampling schedule made it possible to account for the dynamics of inflow and improve interpretation accuracy.

The system demonstrated efficiency under conditions of high mineralization of the production and increased content of mechanical impurities. Compatibility with the existing infrastructure (in particular, with 73-mm tubing and electric submersible pumps) confirms its applicability in mature and watered-out fields. The data obtained formed the basis for subsequent geological and technical analysis and the development of water shutoff solutions.

Figure 2. Inflow Profile from Intervals, m³/day

Figure 3. Interval Water Inflow, %

Figure 4. Interval Oil Inflow, %

Laboratory studies (Figures 2, 3, and 4) revealed significant heterogeneity in the profile: in the interval at the bottomhole, the main water inflow was recorded — 57.7 m³/day of water and 34.9 m³/day of oil, accounting for almost 60% of the total volume; whereas at the wellhead, the values were 21.5 m³/day of water and 6.0 m³/day of oil.

Isolation modelling revealed the following:

  • Isolation of the lower interval reduced water cut by 2.5%, but was accompanied by a loss of 66.2 m³/day of oil.

  • Isolation at the wellhead provided a reduction in water cut by 3.9% with a loss of 32.9 m³/day of oil.

  • Comprehensive isolation of both intervals and bridging of the lower section as a result of sand production provided a total reduction in water cut by 16.1%, but was accompanied by a decline in total production rate of 120.2 m³/day of fluid and 70.6 m³/day of oil.

These results emphasize the need for a strategic approach to water cut management, focusing not only on reducing water inflow but also on maintaining acceptable levels of oil production. Thus, isolation of the zone in interval No. 4 proved to be more preferable in terms of the ratio of water cut reduction to oil loss.

Upon completion of the monitoring, the assembly was successfully retrieved in accordance with the approved plan. The results of the inspection confirmed the technical integrity of all components, which allows the equipment to be reused without additional costs for restoration.

Thus, the presented method combines technological novelty with high practical value, providing an accurate assessment of the inflow profile, a reduction in silting risks, and rapid integration into existing technological processes. Its application contributes to more informed decision-making in conditions of increasing water cut and the complication of geological and production conditions.