Union Jack Oil公司报告称,位于俄克拉荷马州中部的Sark油井在对Prue砂岩层进行为期30天的生产测试后,并未产出具有商业价值的油气。该井钻探至总深度5391英尺,电测井数据显示,在测试前该层存在含油气层段。
为了评估普鲁层段,安装了临时生产设施,但测试结果证实其产量不具备商业可行性。井后分析表明,该层段存在一个有效的构造封闭层,但后来被破坏。
Union Jack持有Sark油井53%的股份。
Union Jack Oil公司报告称,位于俄克拉荷马州中部的Sark油井在对Prue砂岩层进行为期30天的生产测试后,并未产出具有商业价值的油气。该井钻探至总深度5391英尺,电测井数据显示,在测试前该层存在含油气层段。
为了评估普鲁层段,安装了临时生产设施,但测试结果证实其产量不具备商业可行性。井后分析表明,该层段存在一个有效的构造封闭层,但后来被破坏。
Union Jack持有Sark油井53%的股份。

Union Jack Oil reported that the Sark well in central Oklahoma did not yield commercial hydrocarbons following a 30-day production test of the Prue Sandstone. The well was drilled to a total depth of 5,391 ft, with electric logs indicating hydrocarbon-bearing intervals prior to testing.
Temporary production facilities were installed to evaluate the Prue interval, but testing results confirmed that flow rates were not commercially viable. Post-well analysis indicated the presence of a valid structural closure that was later breached.
Union Jack holds a 53% interest in the Sark well.