Interoil 在哥伦比亚成功修井,延长资产寿命

Interoil 的干预使得 Vikingo 油田的石油产量重新回到了 400 桶/天。


该公司 11 月 11 日宣布,Interoil Exploration and Production ASA 的子公司 Interoil Colombia Exploration and Production 已成功完成对哥伦比亚 Vikingo 油井的井下干预。

干预措施包括安装一台操作配置经过改进的喷射泵,使石油产量从干预前的每天 105 桶恢复到每天 400 桶。

虽然预计产量将稳定在 200 桶/天左右,但新的喷射泵配置通过降低提升成本提高了运营效率。

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Interoil Extends Asset Life with Successful Well Intervention in Colombia

Interoil’s intervention brought production at Vikingo well back up to 400 bbl/d of oil.


Interoil Exploration and Production ASA’s subsidiary Interoil Colombia Exploration and Production has successfully completed a downhole intervention to the Vikingo well in Colombia, the company announced Nov. 11.

The intervention included the installation of a jet pump with a modified operational configuration, which restored oil production to 400 bbl/d, an increase from the pre-intervention level of 105 bbl/d.

While production is expected to stabilize at around 200 bbl/d, the new jet pump configuration has improved operational efficiency by reducing lifting costs.

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