Daydream-2 行动更新

来源:www.gulfoilandgas.com 8/29/2024,地点:未分类

要点
• 成功拆除所有临时堵塞物
• 所有区域均开放,气体和完井液流畅通
• 生产测井工具 (PLT) 操作将于本周晚些时候开始

Elixir Energy Limited(“Elixir”或“公司”)很高兴提供其全资拥有的昆士兰州 Taroom Trough 的 Grandis 项目中 Daydream-2 井的运营更新。Daydream

-2 井现已成功拆除其六个独立刺激区之间的所有临时堵塞物。承担这项工作的盘管单元 (CTU) 已交给 Elixir 的邻近运营商。一旦投入测试,井中的气体和完井液即可自由流回地面,无需任何协助。

该井目前处于测试的清理阶段,所有区域均开放,气体和刺激液(水)流畅通通。到目前为止,已从总共抽取的 10,392 桶(占 41%)中回收了 4,300 桶增产液。

本周快结束时,将在井中运行生产测井工具 (PLT)。运行该工具是为了更好地了解井中有多少液体、每个单独区域的流量比例以及各个区域的流动压力。


Elixir 预计,彻底清理油井将需要数周时间,并且可能需要 CTU 返回 Daydream-2 以在测试计划完成之前提起井中剩余的流体。随着清理工作的进展,未来几周将发布进一步公告。Elixir

董事总经理 Neil Young 先生表示:“Daydream-2 计划的最后流量测试阶段继续按计划进行。所有受刺激区域现在都暴露在井眼中,我们将在未来几周继续收集重要数据,以更好地了解 Taroom Trough 多层产油区的巨大潜力。”

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原文链接/GulfOilandGas

Daydream-2 Operation Update

Source: www.gulfoilandgas.com 8/29/2024, Location: Not categorized

HIGHLIGHTS
• All temporary plugs successfully removed
• Well flowing gas and completion fluid with all zones open
• Production logging tool (PLT) operations to begin later this week

Elixir Energy Limited (“Elixir” or the “Company”) is pleased to provide an operational update on the Daydream-2 well in its 100% owned Project Grandis in Queensland’s Taroom Trough.

The Daydream-2 well has now successfully had removed all the temporary plugs between its six separate stimulated zones. The Coil Tubing Unit (CTU) that undertook the work has been released to Elixir’s neighboring Operator. The well flowed gas and completion fluid back freely to surface once it was put onto test, without the need for any assistance.

The well is now in the clean-up phase of the test, flowing gas and stimulation fluid (water) with all zones open. So far, 4,300 barrels of stimulation fluid have been recovered from a total of 10,392 barrels pumped (41%).

Towards the end of the week a production logging tool (PLT) will be run in the hole. This tool will be run to improve the understanding of how much fluid is in the hole, the proportion of flow from each individual zone, and the flowing pressure from the respective zones.


Elixir anticipates that cleaning the well up completely will take several weeks, and may require the CTU to return to Daydream-2 to lift any remaining fluid in the hole before the testing program is completed. Further announcements will follow in the weeks to come as the clean-up progresses.

Elixir’s Managing Director, Mr Neil Young, said: “This final flow testing phase of the Daydream-2 program continues to go to plan. All stimulated zones are now exposed to the wellbore and we will continue to gather vital data over the weeks to come to better understand the massive potential of the multi-stacked pay zones in the Taroom Trough.”

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