Monumental Energy 提供有关新西兰 Copper Moki-1 油气井的最新进展


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Monumental Energy Corp. 宣布,其在 Copper Moki 项目的第二口修井,即位于新西兰塔拉纳基盆地的 Copper Moki-1 (CM-1) 油气井,取得了进展。

Monumental Energy 提供有关新西兰 Copper Moki-1 油气井的最新进展

CM-1 修井的主要目标是恢复 Mt. Messenger 砂层的石油和相关天然气产量,并消除之前作业期间发现的砂层产量流量限制。

在CM-1井,抽油杆柱和旧油管柱已恢复。目前正在清理井筒,并下入新的油管和泵,随后进行额外的射孔。预计工作将于本周末完成,井将投入生产。

CM-1和CM-2的泵将略大一些。每口井的设计产量分别为150桶/天和100桶/天,但在需要时,例如投产后不久的冲洗生产,它们可以运行得更快,以产生更高的产量。

请注意,两口井的冲洗产量总计可达 300 桶/天或更多,这是 Copper Moki 原始钻井计划中最后一次更换泵后 CM2 井的产量。

此前,这些油井钻探时,新西兰面临天然气过剩,该气田一直与天然气管网隔绝。如今,该气田已完全融入天然气基础设施,带来了前所未有的丰厚收益机会。

需要注意的是,CM-1 和 CM-2 最初关闭是由于机械故障,而非任何与储层相关的问题。这些油井只需进行标准维护和更换井下设备即可恢复生产。2024 年底,随着 NZEC 将业务重点转向天然气储存业务模式,Monumental Energy 与 NZEC 达成协议,恢复这些油井的生产。根据协议条款,Monumental Energy 将获得 Copper Moki 油田所有油气产量的 25% 特许权使用费,此前,该公司已全额收回其初始资本投入,并获得了 75% 的特许权使用费。

以石油桶和桶当量为单位的累计产量数据将在未来几周内公布。

 

 

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在线阅读文章:https://www.oilfieldtechnology.com/drilling-and-production/11072025/monumental-energy-provides-update-on-the-copper-moki-1-oil-and-gas-well-in-new-zealand/

 

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原文链接/OilFieldTechnology

Monumental Energy provides update on the Copper Moki-1 oil and gas well in New Zealand

Published by , Editorial Assistant
Oilfield Technology,


Monumental Energy Corp. has announced it has made progress on the second workover in the Copper Moki campaign, i.e., at the Copper Moki-1 (CM-1) oil and gas well, located in the Taranaki Basin, New Zealand.

Monumental Energy provides update on the Copper Moki-1 oil and gas well in New Zealand

The primary objective of the CM-1 workover is to restore oil and associated gas production from the Mt. Messenger sands and to remove flow restriction from sand production identified during prior operations.

At CM-1, the pump rod string has been recovered and the old tubing string has been recovered. Cleaning out the well casing and running the new tubing and pump is now underway followed by the additional perforations. Work is expected to be completed and the well placed into production over the weekend.

CM-1 will have a slightly bigger pump than and that in CM-2. The design rates for each well are 150 bpd of oil and 100 bpd of oil respectively, although they can run faster to generate greater rates than this when required, such as with flush production soon after starting up.

Note that flush production from both wells combined could be 300 bpd of oil or more which was the case for CM2 alone after the last pump replacement at the time of the original drilling program at Copper Moki.

Previously when these wells were drilled, New Zealand faced a gas surplus, and the field remained isolated from the gas network. Today, the field has been fully integrated into the gas infrastructure, presenting a meaningful revenue opportunity that was previously unavailable.

Note that CM-1 and CM-2 were originally shut-in due to mechanical issues, rather than any reservoir-related concerns. The wells have required only standard maintenance, and downhole equipment replacement to be able to resume production. In late 2024, Monumental Energy entered into an agreement with NZEC to bring these wells back online, as NZEC shifted its focus to a gas storage business model. Under the terms of the agreement, Monumental Energy will receive a 25% royalty on all oil and gas production from the Copper Moki site, following full recovery of its initial capital contribution at a 75% royalty.

Cumulative production data, measured in bbl of oil and boe, will be released in the coming weeks.

 

 

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Read the article online at: https://www.oilfieldtechnology.com/drilling-and-production/11072025/monumental-energy-provides-update-on-the-copper-moki-1-oil-and-gas-well-in-new-zealand/

 

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